英文摘要 |
In this study the performances of a laboratory scale membrane bioreactor (MBR) was examined for the aerobic treatment of septic tank effluent. The reactor was with a working volume of 12 L. in continuous operation the suction pump was stopped for 1 minute to allow membrane relaxation after each 5 minutes of filtration to give an average hydraulic retention time (HRT) of 6.48 hours. No sludge was withdrawn during the stage 1 and 2 operations. The SRT of stage 3 and stage 4 was 10 and 20 days respectively. 250 mg/L of NaHCO3 was added for stage 1 and 500 mg/L for stages 2, 3 and 4. The highest removal efficiency of TCOD (total COD), DCOD (dissolved COD) was 96% and 90%, respectively. This study showed that the treatment of septic tank effluent using the laboratory scale aerobic membrane bioreactor was feasible and effective. The results obtained from this study could be applied to the field works and considered as an alternative of household treatment unit for the advance purification of septic tank effluent. |